Well been working alot lately Had a chance to work somemore on the engine. I haven't received the new dist yet so I figure i'd look at what i had. Checked around the intake and noticed DS by #6 was leaking did not notice before. Pulled the intake of the car cleaned everything up put a straight edge on the intake and the heads. Everything good The old gaskets were metal type. Put a better set of gaskets on. and checked the carb while off floats needed adjustment. Carb still not right. But runs better my vacuum is now at 10in my int timing is 18 and my total is 37 My idle is 800rpm Starts better there is i reduse my int timimg say 14 can get 35 but hard starting. I thing with a better carb would solve my problems. Kevin

PS When I hooked the vaccuum gauge to the carb got a vaccuum reading of 5in on the venturi port.

Last edited by 1fastcuda; 03/19/11 11:50 PM.