i think my sprag went....Update With Pic.
#1268545
07/15/12 10:15 PM
07/15/12 10:15 PM
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Joined: Feb 2010
Posts: 1,377 Ohio
Todd
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Last season I had some valve body issues and corrected that with a manual Turbo action cheetah unit. Today I get to the second round start the burnout and roll out in third gear. Get the car staged and take off. Then about 50 feet out it I get a bad chatter in first gear. I shifted to second and feels fine. By that time I know the run is junk so shifted to third and back to the trailer. Got home and drove it in the garage and in first and make ugly sounds really not looking forward to pulling the trans but... I think the sprag took a dump what do you think? Is it possible that it got hurt during the burnout?
Last edited by Todd; 07/21/12 01:26 PM.
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Re: i think my sprag went....
[Re: Todd]
#1268549
07/16/12 10:58 AM
07/16/12 10:58 AM
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Joined: Jan 2003
Posts: 1,142 Central New York
slippery440
Crybaby440
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Crybaby440
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Posts: 1,142
Central New York
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Nice car If it the sprag do yourself a favor and get the sprag with more rollers. I put one in 3 years ago and no problems but I am very carefull about burnouts too.
If the MODS did their job I would not be hitting the notify MOD button. LOL
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Re: i think my sprag went....
[Re: slippery440]
#1268550
07/16/12 01:31 PM
07/16/12 01:31 PM
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Joined: Feb 2010
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Todd
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A few years ago when the trans was built we put a sprag in with all the extra rollers. In the video that was 2 runs prior to Didn't get any video of when it happend.
Last edited by Todd; 07/16/12 01:38 PM.
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Re: i think my sprag went....
[Re: Todd]
#1268551
07/16/12 01:52 PM
07/16/12 01:52 PM
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Joined: Aug 2010
Posts: 632 Casco, MI
Savoy1964
mopar
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mopar
Joined: Aug 2010
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Casco, MI
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with drive shaft disconnected transmission in neutral try turning the end to the right then left if it turns easy in both directions i would think the sprag is shot. if you have an spare slip yoke use that to turn it or the drive shaft itself
2003 Dodge 3500 Diesel
1964 Plymouth Savoy White 2dr sdn. 512 stroked, Dominator, New Best 9.75 @ 138.50mph 2019 Challenger Scat Pack 1320 White Knuckle-K&N Cold air filter, Billit Oil catch can, drag radials stock 11.911 @ 114mph
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Re: i think my sprag went....
[Re: Todd]
#1268554
07/17/12 09:29 AM
07/17/12 09:29 AM
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Joined: Jun 2003
Posts: 52,972 Romeo MI
MR_P_BODY
Master
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Master
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Romeo MI
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Quote:
Pulled the pan and found what looks like ground up springs out of the sprag.
Thats what it looks like.... well its time to pull the trans.... bummer
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Re: i think my sprag went....
[Re: MR_P_BODY]
#1268555
07/17/12 01:08 PM
07/17/12 01:08 PM
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Joined: Feb 2010
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Todd
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Quote:
Quote:
Pulled the pan and found what looks like ground up springs out of the sprag.
Thats what it looks like.... well its time to pull the trans.... bummer
I started on it last night gonna finish tonight after work then off to the trans guy. How much of that stuff got in the converter?
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Re: i think my sprag went....
[Re: MR_P_BODY]
#1268556
07/17/12 01:14 PM
07/17/12 01:14 PM
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Joined: Feb 2010
Posts: 1,377 Ohio
Todd
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Quote:
Quote:
Pulled the pan and found what looks like ground up springs out of the sprag.
Thats what it looks like.... well its time to pull the trans.... bummer
I started to pull it last night probibly finish tonight after work. How much of that stuff got in the converter?
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Re: i think my sprag went....
[Re: mopar400]
#1268560
07/17/12 08:12 PM
07/17/12 08:12 PM
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Joined: Feb 2010
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Todd
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Re: i think my sprag went....
[Re: Todd]
#1268562
07/18/12 10:18 AM
07/18/12 10:18 AM
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Joined: Jan 2003
Posts: 16,928 NC
440Jim
I Live Here
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I Live Here
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NC
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Quote:
A few years ago when the trans was built we put a sprag in with all the extra rollers. In the video that was 2 runs prior to Didn't get any video of when it happend.
So the trans already has either the A&A Ultimate sprag or the Coan Super sprag with 16 rollers? (vs the 12 roller Chryser).
It is likely that the valve body can be changed to low band apply, check with John Cope at CRT. He has done some in the past, but not all valve bodies can be changed.
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Re: i think my sprag went....found stuff in pan...
[Re: Todd]
#1268563
07/18/12 10:33 AM
07/18/12 10:33 AM
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Joined: May 2003
Posts: 13,200 aZLiViN
J_BODY
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I Live Here
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Quote:
Last season I had some valve body issues and corrected that with a manual Turbo action cheetah unit.
....so are we sure the t/a valve body "corrected" the issue you were having? You just don't hear of this issue much with their manual valve body being used. I know I never had issues with mine. Too bad I don't live near you. Sold my race car, but still have the "back up" trans sitting here which I used for years prior to going full race trans. It has a TA valve body and I never had sprag issues.
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Re: i think my sprag went....found stuff in pan...
[Re: J_BODY]
#1268564
07/18/12 11:07 AM
07/18/12 11:07 AM
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Todd
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Quote:
Quote:
Last season I had some valve body issues and corrected that with a manual Turbo action cheetah unit.
....so are we sure the t/a valve body "corrected" the issue you were having? You just don't hear of this issue much with their manual valve body being used. I know I never had issues with mine. Too bad I don't live near you. Sold my race car, but still have the "back up" trans sitting here which I used for years prior to going full race trans. It has a TA valve body and I never had sprag issues.
Thanks for the offer. The prior valve body was a homemade manual one that a buddy had laying around let me try. Some times it it would work fine and the next pass wouldnt leave in first gear. After changing to the turbo action unit been fine. Its got around 30 passes on this one with no problems until now.
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