my 3.9 still sucks..UPDATED
#58846
05/16/08 11:59 PM
05/16/08 11:59 PM
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Joined: Dec 2003
Posts: 5,314 Carstairs, Alberta, Canada
dave571
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OP
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Joined: Dec 2003
Posts: 5,314
Carstairs, Alberta, Canada
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OK...I've got a 3.9 that runs like a bag of you know what. 96 ram 1500 2wd 5 speed. Very poor idle, and stumble off idle. Almost sounds like it's missing on a cylinder or 2, but it's not(verified on ociliscope) Here's what I've found it's NOT -plugs -cap -rotor -wires -coil -all sensors seem to be working within thier normal range. O2 sensor is new. -valves are not sticking -converter is not plugged -fuel pressure and volume are good -Compression is present. 120 psi on the left, around 90 on the right. I've blamed the discrepency on temp varience between the sides while testing. -Timing chain was completely terrible (1" of deflection) replaced it. runs the same. -have checked for external vac leaks. None found I've heard a few guys say the intakes are known to crack on these, but I've never heard of it. Still have to follow up on it. PCM ? Any idea's welcomed.
Last edited by dave571; 06/09/08 11:19 PM.
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Re: my 3.9 still sucks
[Re: dave571]
#58847
05/17/08 12:23 AM
05/17/08 12:23 AM
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Joined: Aug 2005
Posts: 4,861 Riverside, Ca
R70RUNNER
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master
Joined: Aug 2005
Posts: 4,861
Riverside, Ca
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I've never done it, I have a 2000 3.9 and the swap only works up to 1999, but it was quite fashionable to install the the Ford Motorsports 19# injectors in those engines... Direct swap, the improvement was the Ford injector had 4 holes for spray vs. the OEM Mopar's single hole. On the Dakota board guys were reporting much improvement in idle quailty and low speed smoothness in the 3.9's with the injector change, and they were pretty cheap, 8 injectors for less then $100 IIRC. Google "Ford injectors in 3.9 Dodge" should bring up some threads that have more info. EDIT: Those are the 4.6 V8 injectors
Last edited by R70RUNNER; 05/17/08 12:28 AM.
Current cars: 2000 Dak Quad Cab, 2012 Challenger,1970 Road Runner, 1994 Firehawk
1966 Coronet post sedan, 1988 Corvette, 2005 Magnum RT all SOLD
R70RUNNER<---VP Inland Empire Chapter of the MPM
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Re: my 3.9 still sucks
[Re: dave571]
#58850
05/17/08 02:04 PM
05/17/08 02:04 PM
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Joined: Jan 2005
Posts: 12,419 Kalispell Mt.
HotRodDave
I Live Here
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I Live Here
Joined: Jan 2005
Posts: 12,419
Kalispell Mt.
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I still think it's probably the ECU.
However you need to double check your compression readings because the 90 is very low even stone cold. Did you check it with all the plugs out?
I am not causing global warming, I am just trying to hold off a impending Ice Age!
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Re: my 3.9 still sucks
[Re: HotRodDave]
#58851
05/17/08 02:41 PM
05/17/08 02:41 PM
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Joined: Mar 2006
Posts: 1,611 Pataskala, Ohio
GTX70sixpack
top fuel
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top fuel
Joined: Mar 2006
Posts: 1,611
Pataskala, Ohio
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The intermediate shaft bushing wears out and causes the distributor to jump, can even ruin the distributor. Used to replace them all the time. Remove the distibutor and use a long wide blade screwdriver to see if you have any side play in the gear.
65 Belvedere II Station Wagon 69 Coronet R/T convertible 70 GTX 70'cuda 99 Dodge Diesel dually 4X4
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Re: my 3.9 still sucks
[Re: GTX70sixpack]
#58852
05/17/08 05:59 PM
05/17/08 05:59 PM
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Joined: Dec 2003
Posts: 5,314 Carstairs, Alberta, Canada
dave571
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Joined: Dec 2003
Posts: 5,314
Carstairs, Alberta, Canada
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I'm starting to question the ecu as well, but only as a last resort. I have seen lot's of ecus replaced over the years, with only about 1% actually fixing anything.
I'm going to spend some time verifying that the distributor is actually timed right(that no one has messed with it). Would seem to be a good time to pull it out and inspect it too.
Replacing the timing chain with 1" of slack did make a difference in above 2000 rpm performance, but it is still far from fixed. The fact that it changed at all, could ad some credibility to the distributor gone bad theory.
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Re: my 3.9 still sucks
[Re: AdamR]
#58854
05/19/08 01:18 AM
05/19/08 01:18 AM
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Joined: Mar 2006
Posts: 1,611 Pataskala, Ohio
GTX70sixpack
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top fuel
Joined: Mar 2006
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Pataskala, Ohio
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Quote:
My 98 Dakota has a 3.9L, Its a pig, I cant imagine how slow it must be in a ram, though the 5 speed may help.
My 98 Dakota runs very well, I was in W.Va. with a 700 lb. quad in the back and my friend had his 97 Chebie 1500 4X4 with a 350 and a 700 lb. quad, we stopped at a light side by side starting up a large grade, he asked if I wanted to race and I said your on, expecting to get stomped. By the time I hit third gear he was 8 cars back. Mine is a 5 spd and his a heavier 4X4 butt the difference was unbelivable. Another freinds 97 Dodge 1500 4X4 with a 360 Magnum isn't much quicker than the Chevie.
65 Belvedere II Station Wagon 69 Coronet R/T convertible 70 GTX 70'cuda 99 Dodge Diesel dually 4X4
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Re: my 3.9 still sucks
[Re: dave571]
#58856
05/19/08 09:04 PM
05/19/08 09:04 PM
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Joined: Jul 2003
Posts: 6,167 Maryland
GO_Fish
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Posts: 6,167
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Is the exhaust hissing? The honeycomb brick broke up inside my cat on my old '90 Dak. Pieces of the cat blew downstream and clogged the muffler. Power was very low and exhaust pushing backwards melted my EGR valve a few times before I figured it out. My final clue? Pissed off at no power and not figuring out, I just mashed the pedal to the floor and just held it there. POW!!! Blew a hole in the side of the muffler, then the power came back!
Scott B.
"I'm a self-made man... I started with nothing, and I still have most of it!"
68 360 rusty B'cuda 'vert (GO Fish)13.59@ 98.72 mph
69 340 GTS stock 14.18@ 95.60 mph
01 5.9L Ram 1500 Quad Cab 4x4
01 3.5L 300M 16.23@ 86.97 mph
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Re: my 3.9 still sucks
[Re: dave571]
#58857
05/19/08 09:57 PM
05/19/08 09:57 PM
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Joined: Jan 2007
Posts: 1,668 Mi,U.S.A.
mike s
top fuel
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top fuel
Joined: Jan 2007
Posts: 1,668
Mi,U.S.A.
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Sounds like a couple things.1.As earlier mentioned replace the dist drive /intermediate shaft 2.The plenum gasket is likely leaking. (It seals the bottom of the intake manifold).BTW they do not crack they blow the gasket out.KRC Performance and Hughes Engines offer a replacement plate that will stop the gasket from failing again.
Leave the gun.......take the Cannoli's....Mike
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Re: my 3.9 still sucks
[Re: jeepers007]
#58860
05/20/08 12:25 AM
05/20/08 12:25 AM
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Joined: Dec 2003
Posts: 5,314 Carstairs, Alberta, Canada
dave571
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OP
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Joined: Dec 2003
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Carstairs, Alberta, Canada
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GO_Fish .... the muffer was completely rusted off, when I got the truck (it was already running like it does now). I replaced it. Then as I became frustrated with the running, I thought it was the converter, so I cut it open to look inside. Already empty so I don't think that's it. Thanks though.... mike_s ..... I'll check some more for vac leaks at the plennum, but I've already looked around there quite a bit. I'm hoping that chcking into the distributor will turn into something. BIGBLOCK78DOBA .... "Sorry to hear your 3.9 dak is bumming you out!! MY 5.2 '94 DAK IS a rocket ship,glad I didn't go with the 3.9. " Actually mine is a Full size, so at least it has THAT going for it
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Re: my 3.9 still sucks
[Re: bbtrux]
#58862
05/20/08 11:29 PM
05/20/08 11:29 PM
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Joined: Sep 2003
Posts: 107 AZ and UT
Bill55AZ
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Posts: 107
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If the plenum gasket is bad, the crankcase will be under a slight vacuum instead of a slight pressure. With engine idling in park, remove pcv and crankcase breather cap from valve covers. cover the holes with your hands for about 5 seconds, then lift one hand. Direction of air will tell you if the gasket is bad. If it sucks in, replace the gasket....
1979 Volare Wagon "chick magnet" sold and in the Netherlands (really)
1980 LeBaron Coupe current project
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Re: my 3.9 still sucks
[Re: Bill55AZ]
#58863
05/21/08 12:04 AM
05/21/08 12:04 AM
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Joined: Dec 2003
Posts: 5,314 Carstairs, Alberta, Canada
dave571
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Thanks for the further input guys I see what you mean about the height. It's one piece from the head up to the throttle plates. The bolt on plate is underneath right? so you have to pull the intake to get to it ? In any case, with the cap off, I cannot feel any play in the distributor.(at least not slop side to side etc). I can feel some rotational movement, much like I would expect to feel on a v8 in the slot/drive. It doesn't seem excessive. I pulled the throttle plate assembly this evening and notice there is a ton of carbon in it. Nothing that strikes me as abnormal. Perhaps pulling the intake is the next step for me right now. Cheers
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Re: my 3.9 still sucks
[Re: FuryUs]
#58865
05/25/08 09:31 PM
05/25/08 09:31 PM
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Joined: Dec 2003
Posts: 5,314 Carstairs, Alberta, Canada
dave571
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UPDATE it still sucks pulled intake. No evidence of plate leakage, or gasket leakage. Replaced it all anyway. still the same. Pulled dist at same time. No bushing play at all. Egr valve is a blockoff plate, so that's not it either. I'll keep pulling my hair out...er I mean digging.
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