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STUPID QUESTION #1456586
06/22/13 04:27 PM
06/22/13 04:27 PM
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Now - Port Orange,Fla. Former...
MIKES_DUSTER Offline OP
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I just had a BIG problem(big for me) with my new motor. I want to check and see if my oil pump is worrying,which way do iI spin it, clock-wise or counter clock-wise????

Re: STUPID QUESTION [Re: MIKES_DUSTER] #1456587
06/22/13 05:00 PM
06/22/13 05:00 PM
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up yours
Supercuda Offline
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Same direction as the distributor.

BB - looking at the hex CCW
SB - looking at the hex CW


They say there are no such thing as a stupid question.
They say there is always the exception that proves the rule.
Don't be the exception.
Re: STUPID QUESTION [Re: Supercuda] #1456588
06/22/13 05:04 PM
06/22/13 05:04 PM
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Posts: 6,301
colorado
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a12superbee Offline
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colorado
When you pull the drive out make sure you didn't twist the tip off of the shaft.


I can't afford this. mark
Re: STUPID QUESTION [Re: a12superbee] #1456589
06/22/13 06:15 PM
06/22/13 06:15 PM
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Now - Port Orange,Fla. Former...
MIKES_DUSTER Offline OP
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Dist. and bronze gear out,now just want to make sure my oil pump is working. Brand new motor with maybe 5 miles on it doesn't have oil pressure. I found a BIG problem, on drivers side,a rocker adjuster broke and on pass side, a rocker adjuster nut came off and both are in my motor. Will be taking the intake off next week.

Re: STUPID QUESTION [Re: MIKES_DUSTER] #1456590
06/22/13 07:34 PM
06/22/13 07:34 PM
Joined: May 2003
Posts: 6,562
Downtown Roebuck Ont
Twostick Online content
Still wishing...
Twostick  Online Content
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Downtown Roebuck Ont
If it spit a lifter out of it's bore in the process, that's where your oil pressure might have went.

Kevin

Re: STUPID QUESTION [Re: Twostick] #1456591
06/22/13 08:39 PM
06/22/13 08:39 PM
Joined: Nov 2003
Posts: 36,040
Lincoln Nebraska
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RapidRobert Offline
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Lincoln Nebraska
Quote:

If it spit a lifter out of it's bore in the process, that's where your oil pressure might have went. Kevin


X2, since you wouldn't lose psi just from the rocker nut(s) coming apart. I'm thinking you shut it down when the cyls started acting up & that'd of saved it from the no oil psi damage. retrieve the parts/solve the rocker issue & you'll likely come out of this in good shape. It was not a dumb Q. What eng? I'd fix the rockers then preoil with a 5/16" hex with the crank turned to the 2 seperate sweet spots to confirm the heads are oiling plus what you see on your gauge. The big problem/issue/question mark is what happened to the rocker assys'


live every 24 hour block of time like it's your last day on earth
Re: STUPID QUESTION [Re: RapidRobert] #1456592
06/22/13 09:53 PM
06/22/13 09:53 PM
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MIKES_DUSTER Offline OP
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Its a 360. I must have shut it off right in time because it didn't make any loud noises and sounded ok.

Re: STUPID QUESTION [Re: MIKES_DUSTER] #1456593
06/22/13 10:16 PM
06/22/13 10:16 PM
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MIKES_DUSTER Offline OP
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Ok guys......just went out to prime the motor to see what happens. The oil pressure kept going up and down. It jumped to 20 and then stayed at 10. The pass side had oil coming out of the head but none out of the drivers side.
The drivers side has the broken adjuster and the pass side has the missing adjuster nut.

Re: STUPID QUESTION [Re: MIKES_DUSTER] #1456594
06/22/13 10:26 PM
06/22/13 10:26 PM
Joined: Nov 2003
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Lincoln Nebraska
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RapidRobert Offline
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Quote:

The oil pressure kept going up and down. It jumped to 20 and then stayed at 10. The pass side had oil coming out of the head but none out of the drivers side.


(1) the leak still ain't plugged (2) need to turn the crank with a 1&1/4" socket/breaker bar till you hit the spot where the dr head oils but first cap the leak


live every 24 hour block of time like it's your last day on earth
Re: STUPID QUESTION [Re: RapidRobert] #1456595
06/22/13 10:47 PM
06/22/13 10:47 PM
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MIKES_DUSTER Offline OP
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I don't understand when you say, The leak isn't plugged yet???

Re: STUPID QUESTION [Re: MIKES_DUSTER] #1456596
06/22/13 10:56 PM
06/22/13 10:56 PM
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Lincoln Nebraska
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RapidRobert Offline
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Drill priming or even hand priming will kick up far in excess of the 10lbs you are showing. Either a lifter is out of its' bore or a gallery plug is missing or there's an issue on the suction side (pickup/pump regulator)


live every 24 hour block of time like it's your last day on earth
Re: STUPID QUESTION [Re: RapidRobert] #1456597
06/22/13 11:07 PM
06/22/13 11:07 PM
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MIKES_DUSTER Offline OP
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Everything is new in the motor and everything was fine. It usually has 70lbs but the other day,idling in my garage it had 0.

Re: STUPID QUESTION [Re: MIKES_DUSTER] #1456598
06/22/13 11:26 PM
06/22/13 11:26 PM
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gulfport, ms, west mi
rowin4 Offline
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The lifter popped out when the push rod dropped off. Don't try running it until you find the problem. NO OIL PRESSURE means NO OIL !!!!!!!!


it's ok to butt heads, just don't do it with a butthead
Re: STUPID QUESTION [Re: rowin4] #1456599
06/22/13 11:38 PM
06/22/13 11:38 PM
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Now - Port Orange,Fla. Former...
MIKES_DUSTER Offline OP
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Oh,I'm NOT running it!!!!!! I find it hard to believe that a roller lifter that is connected to another roller lifter can come out of the bore. Unless the bar broke.

Re: STUPID QUESTION [Re: MIKES_DUSTER] #1456600
06/23/13 12:06 AM
06/23/13 12:06 AM
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Posts: 36,040
Lincoln Nebraska
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RapidRobert Offline
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Didn't know it was roller lifters. Mike, holler what it ends up being


live every 24 hour block of time like it's your last day on earth
Re: STUPID QUESTION [Re: MIKES_DUSTER] #1456601
06/23/13 12:09 AM
06/23/13 12:09 AM
Joined: Mar 2008
Posts: 5,746
Ontario, Canada
Dodgem Offline
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I kicked a roller lifter out last year and it stayed up above the oil hole (bar bent a bit) and had 0 oil pressure so it can happen!

Re: STUPID QUESTION [Re: Dodgem] #1456602
06/23/13 12:27 AM
06/23/13 12:27 AM
Joined: Jun 2012
Posts: 1,899
MYRTLE BEACH SOUTH CAROLINA
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ek3 Offline
top fuel
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I have run in to a a case where I lost all oil pressure suddenly on [forgive me ] a 355 chev. racing engine . during a qualifiying lap it dropped from 70 lbs to 0 . i came in and we checked it over .it would go up and down when reved to only about 10 lbs... turned out to be an imploaded oil filter . happened several times . I had to use an Oberg screen system and not over a 20-50 race oil to control it .

Re: STUPID QUESTION [Re: RapidRobert] #1456603
06/23/13 01:06 AM
06/23/13 01:06 AM
Joined: Jan 2003
Posts: 9,146
Now - Port Orange,Fla. Former...
MIKES_DUSTER Offline OP
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Will do Robert. Dodge,Were you racing it or driving your car when it happened??? My duster was idling in the garage. Not saying it couldnt happen idling but sounds weird if it did. Im wondering now if the broken rocker adjuster could have cause the lifter bar to bend or break???







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