Well it turns out I was mistaken. The crankshaft key was not sheared. Only the camshaft key was broke. So I pulled the crank gear off for nothing. Some of the ugliness of those threads in the crank is residual loctite. I just got back from town, had to run for a woodruff key. Hopefully I'll know something pretty soon. Now I need to pull out my paperwork and figure out how I time this gear drive again.


[img]http://i.imgur.com/boeexFms.jpg[/img]
31 Plymouth Coupe, 392 Hemi, T56 magnum
RS23J71
RS27J77
RP23J71
RO23J71
WM21J8A
I don't regret the things I've done. I only regret the things I didn't do.
"Wise men talk because they have something to say; fools because they have to say something. ~ Plato"