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Theory anyone? #437542
08/14/09 08:28 AM
08/14/09 08:28 AM
Joined: Jan 2007
Posts: 531
Charlotte, NC
Kowal Offline OP
mopar
Kowal  Offline OP
mopar

Joined: Jan 2007
Posts: 531
Charlotte, NC
Anyone want to try to guess what just happened to my 383 car?

Driving home from Woodward last night. On the highway, about 70 mph, 3200 rpm. Nice night, running great. ALL OF THE SUDDEN....lost power as if I stalled, then BANG, an extremely loud backfire out the exhaust. Ran "alright" afterward but with less acceleration power.

Got near my house about 15 minutes later, got off the highway and the car immediately stalls. I play around with it by the side of the road (swapped orange box, ballast and coil) and it won't start until, later, it finally does but after what I think was the engine cooling down. But now it sounds like something barely audible that is "rattling" or slightly knocking from the motor. There is no readily heard miss, I just "idled" it home and in to the garage.

I know I broke something...probably valve train and maybe other collaterial damage. Just interested in ideas of what I did before I start ripping in to it.

Got any? Bone stock 383, only an Edelbrock and electronic ignition as mods. Oh...to add to the fun, it was after midnight. Also, I have to recognize the Northville, Michigan police, who kept coming by to see if I (and my wife who brought the parts up) were OK.


'69 Hemi Charger 500, ‘70 U code Challenger R/T
(These and a bunch others at www.dkowal426.com)

P.J. O'Rouke: "The old car ran perfectly, right up until it didn't."
Re: Theory anyone? [Re: Kowal] #437543
08/14/09 08:56 AM
08/14/09 08:56 AM
Joined: Jan 2003
Posts: 5,138
East Aurora (Buffalo) NY
RoadRunner Offline
master
RoadRunner  Offline
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Joined: Jan 2003
Posts: 5,138
East Aurora (Buffalo) NY
1. Timing chain skip/broke tooth?
2. Sheared pin of the front of cam allowing it to slip out of phase some, resulting in valves kissing the pistons?
3. Broken rotor under distributor cap?

Let me think some more, I may have others.


68 Road Runner (383/4speed, post car w/decor pkg) - Major Project
69 Road Runner w/472 Hemi & 4 speed.
70 Challenger R/T SE EF8 w/ V9J, U - A32 - Major Project
2023 Ford Mach 1
Re: Theory anyone? [Re: RoadRunner] #437544
08/14/09 09:13 AM
08/14/09 09:13 AM
Joined: Oct 2003
Posts: 7,506
Az
Crizila Offline
master
Crizila  Offline
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Az
Broke valve spring / retainer / keeper. Pull the valve covers first.


Fastest 300
Re: Theory anyone? [Re: Crizila] #437545
08/14/09 10:04 AM
08/14/09 10:04 AM
Joined: Nov 2003
Posts: 36,040
Lincoln Nebraska
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RapidRobert Offline
Circle Track
RapidRobert  Offline
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Posts: 36,040
Lincoln Nebraska
After(as said) taking a peak under the valve covers I'd do a compression test


live every 24 hour block of time like it's your last day on earth
Re: Theory anyone? [Re: RapidRobert] #437546
08/14/09 10:45 AM
08/14/09 10:45 AM
Joined: Mar 2003
Posts: 18,678
Fresno, CA
Jim_Lusk Offline
I Live Here
Jim_Lusk  Offline
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Joined: Mar 2003
Posts: 18,678
Fresno, CA
I initial description has me thinking the bulkhead connector, specifically the ignition circuit unless you lost headlights/radio/etc. at the same time, then it would be the main feed.

That could cause more problems if the ignition came back with cylinders full of fuel.

Check the bulkhead then the engine. I agree with pulling valve covers and doing a comp check.

Re: Theory anyone? [Re: Jim_Lusk] #437547
08/14/09 04:04 PM
08/14/09 04:04 PM
Joined: May 2003
Posts: 15,487
Florida
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scratchnfotraction Offline
I Live Here
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Posts: 15,487
Florida
roll it over by hand and check damper at TDC,look at the rotor and see where its at compaired to #1 plug wire

do that first,then pull vc and check for bent push rods,broke springs,retainers

check the springs before trying to run it any more,so it dont drop a valve if one "IS" broken

then do a comp test

post results and finding please

Re: Theory anyone? [Re: scratchnfotraction] #437548
08/14/09 05:15 PM
08/14/09 05:15 PM

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Anonymous
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I'm guessing it slipped a cog on the timeing chain...

Re: Theory anyone? #437549
08/14/09 07:29 PM
08/14/09 07:29 PM
Joined: May 2008
Posts: 329
tx
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craigsmytcudas Offline
enthusiast
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tx
I concur with all previous posts first . But if the car layed down then kicked back i would have to ask is the fuel pump leaking into the crank case and did it blow up in the block and just think it was from the exhaust. my wife had this happen several years ago the car ran when it cooled but the valve covers were junk and the vally pan was destroyed but low fuel pressure made the car seem weak . c

Re: Theory anyone? #437550
08/14/09 07:34 PM
08/14/09 07:34 PM
Joined: Feb 2008
Posts: 992
Simi Valley, CA
MoparJ Offline
super stock
MoparJ  Offline
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Joined: Feb 2008
Posts: 992
Simi Valley, CA
This seems like a possible electric issue, possibly some kind of power wire providing power to the ignition box may have shorted, or burnt, causing a weak feed. This may cause it to get some power to the box, but not as much as needed for max performance.

This has happened to me before. Crusing about 70 on the hwy; next, I lose fire and get a large pop out of the exhaust. I stop the car and open the hood to find an alt power wire that runs to the wires providing power to the ignition box smoking. Being in a hurry to get to a cruise I was going to, I cranked the motor over and it fired up. Ran ok the rest of the day, then acted up, just as I got the car into the garage. This is when I found the carnage. Another wire it the connector on the right side of the motor arched off of the alt wire. Both had very small slits in them, explaining why they arched.

I replaced both wires and have been ok since.


If it isnt electrical, I would look at upper valvetrain, such as a rocker, or broken spring. Check electric and valvetrain, to be safe.


2016 Ram 1500 Crew Cab: 5.7, 65RFE, 4.56 gears with locker, Hemifever tuned, AFE intake, 87mm throttle body, JBA headers, 3" Flowmaster exhaust, split to dual 2.5" exits. 13.57 best ET so far.

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Re: Theory anyone? [Re: Kowal] #437551
08/14/09 08:10 PM
08/14/09 08:10 PM

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Does it continue to stall or "die" after the engine gets hot, then only starts after sitting for a while and cools down? If so, my first guess is the pick-up coil in the dist. Next time it stalls check the ohms on the pick-up before it has a chance to cool down and make sure it's ok.

Re: Theory anyone? (update) #437552
08/15/09 10:15 PM
08/15/09 10:15 PM
Joined: Jan 2007
Posts: 531
Charlotte, NC
Kowal Offline OP
mopar
Kowal  Offline OP
mopar

Joined: Jan 2007
Posts: 531
Charlotte, NC
First update...

Today I did all the mechanical checks...

Engine turns over nice and easy with the plugs removed, no sounds or tight spots.

Distributor gear lines up with the crank correctly at TDC, so timing chain seems OK

Took the valve covers off, everything is intact.

Did a compression check, all was remarkably consistent and good.

Thank God! Seems like mechanically I am OK.

Tomorrow I will play with the electical. One thing I noticed...the distributer rotor to cap wear doesn't seem right. The end of the rotor and 8 contacts on the cap seem unusually worn for a car not driven much.

Harness is original and also getting too old, may have to spring for a replacement. The firewall junction block does seem OK though, tight and no burn marks between the connectors.

As I noted above, I did replace the coil, orange box and ballast and yet the car didn't start until after it cooled. Odd. Distributor does seem suspect (not much left to swap!)


'69 Hemi Charger 500, ‘70 U code Challenger R/T
(These and a bunch others at www.dkowal426.com)

P.J. O'Rouke: "The old car ran perfectly, right up until it didn't."
Re: Theory anyone? (update) [Re: Kowal] #437553
08/16/09 12:21 AM
08/16/09 12:21 AM
Joined: Sep 2006
Posts: 2,587
missouri, USA
moparmojo Offline
master
moparmojo  Offline
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Joined: Sep 2006
Posts: 2,587
missouri, USA
I wont pretend to tell you I have the answer. But when you described your problem it sounded exactly like what happened to my Challenger years ago. The only main difference was that I was doing 95-100mph on the highway for an extended period of time (yes, I was driving like an idiot).

Anyway, car was driving fine at a nice click, when I lost power and heard a bang. I let off the throttle. Car was still running and heard nothing more. Gently got back in it and drove the other hour home from the Ozarks. When I got off the highway, I stopped to pick up a soda at the local fast food joint and noticed the car was making a rattle. Sounded like valve train. By the time I got home it was more noticable. The next morning I had trouble getting it restarted. I thought it was bad lifters so I changed them all. Still did not fix the issue, but it was at have the engine speeds as the motor sound. I was never happy with the motor after than and ended up having it rebuilt into my stroker. Still dont know what went wrong, but my piston skirts were all scored and I found the cam difficult to get out of the bore. Other than that, it is still a mystery. Ive heard of torque converter ballooning but dont know if that happened here.

Re: Theory anyone? #437554
08/16/09 12:57 AM
08/16/09 12:57 AM
Joined: Jul 2003
Posts: 1,107
Spring Valley ,Ca.
moparsquid Offline
super stock
moparsquid  Offline
super stock

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Posts: 1,107
Spring Valley ,Ca.
Quote:

I'm guessing it slipped a cog on the timeing chain...


i had a 72 dodge truck with a 440 in it and i was a block away from home when it coughedand shut down got it started but only ran on like 4 cylinders. pulled t/c cover and found cam gear had torn open and looked like mr packman.r/r it and it ran fine.

Re: Theory anyone? [Re: moparsquid] #437555
08/16/09 01:01 AM
08/16/09 01:01 AM
Joined: Mar 2003
Posts: 18,678
Fresno, CA
Jim_Lusk Offline
I Live Here
Jim_Lusk  Offline
I Live Here

Joined: Mar 2003
Posts: 18,678
Fresno, CA
Just because the bulkhead seems tight doesn't mean the connectors are tight. You need to look closely and the dash harness end. The curled over parts will open up and need to be closed back up. It's a lot of work, but it will take care of lots of gremlins.

Re: Theory anyone? [Re: Jim_Lusk] #437556
08/16/09 01:08 AM
08/16/09 01:08 AM
Joined: Feb 2003
Posts: 10,208
Someplace you aren't
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SomeCarGuy Offline
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SomeCarGuy  Offline
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Posts: 10,208
Someplace you aren't
A YO harness is never a bad investment if your hasn't been replaced before.

I got one for my 69 RR for 85 bucks this summer with the Moparts discount. A KILLER piece.


I want my fair share
Re: Theory anyone? [Re: SomeCarGuy] #437557
08/16/09 09:14 AM
08/16/09 09:14 AM
Joined: Jan 2003
Posts: 1,663
E.Amherst, NY
69RR Offline
top fuel
69RR  Offline
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Joined: Jan 2003
Posts: 1,663
E.Amherst, NY
Same thing happened to me in my 69 RR 383. I was racing (I know..I know) a z06 vette (that was stupid..I know,I know). I hit second gear and shifting into 3rd hard it went "BANG" and next thing I'm over the side of the road (my muffler took a beating) . It would turn over but not start.

Looking at it at home I found out the mechanical advance had jammed and my reluctor had sheered. Somehow the distributor must have wobbled or shifted when I did a bonzai shift.

New distributor and was good to go.


Dean Got my hands on the wheel, foot to the pedal, gonna drive this car till the tires turn to metal - gonna sleep when I'm dead and laugh at the devil..
Re: Theory anyone? (update) [Re: Kowal] #437558
08/16/09 02:24 PM
08/16/09 02:24 PM

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Anonymous
Unregistered
Anonymous
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Quote:

First update...

Today I did all the mechanical checks...

Engine turns over nice and easy with the plugs removed, no sounds or tight spots.

Distributor gear lines up with the crank correctly at TDC, so timing chain seems OK

Took the valve covers off, everything is intact.

Did a compression check, all was remarkably consistent and good.

Thank God! Seems like mechanically I am OK.

Tomorrow I will play with the electical. One thing I noticed...the distributer rotor to cap wear doesn't seem right. The end of the rotor and 8 contacts on the cap seem unusually worn for a car not driven much.

Harness is original and also getting too old, may have to spring for a replacement. The firewall junction block does seem OK though, tight and no burn marks between the connectors.

As I noted above, I did replace the coil, orange box and ballast and yet the car didn't start until after it cooled. Odd. Distributor does seem suspect (not much left to swap!)




Have you checked or replaced the pick-up coil in the distributor yet?

~Jimmy

Re: Theory anyone? #437559
08/16/09 02:41 PM
08/16/09 02:41 PM
Joined: Apr 2008
Posts: 233
WV,USA
W
wvmarv Offline
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wvmarv  Offline
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WV,USA
Sounds right to me. To backfire, probably has cam sprocket with plastic teeth worn out.

Re: Theory anyone? [Re: Kowal] #437560
08/16/09 02:49 PM
08/16/09 02:49 PM
Joined: Dec 2008
Posts: 938
Poplar Bluff, Mo. 63901
2
268RTs4ME Offline
super stock
268RTs4ME  Offline
super stock
2

Joined: Dec 2008
Posts: 938
Poplar Bluff, Mo. 63901
I would check my distributor now, unevenwear on the inside of your caps should tell you something, possible bad bushing, at high rpm, missfired, could cause you alot of troble and expense, If you have another dist. switch and see what results you get.keep inform..

Re: Theory anyone? [Re: Kowal] #437561
08/16/09 03:37 PM
08/16/09 03:37 PM
Joined: Oct 2007
Posts: 288
Birmingham, England
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Mick70RR Offline
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Joined: Oct 2007
Posts: 288
Birmingham, England
A similar thing happened to me some time ago and I managed to limp the car home. First thing I did was check the timing and it was retarded but the dizzy was clamped up tight. Turned out the roll pin that holds the reluctor in place has sheared in two and the reluctor had moved on the shaft.


1970 Road Runner 505 cid MCH CNC ported Stealth heads MP 528 camshaft 4 speed GV overdrive 11.98 @ 117 on street treads
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