Re: 518 OD not engaging
[Re: BDW]
#3091840
11/05/22 01:46 PM
11/05/22 01:46 PM
|
Joined: Sep 2003
Posts: 19,687 north of coder
moparx
"Butt Crack Bob"
|
"Butt Crack Bob"
Joined: Sep 2003
Posts: 19,687
north of coder
|
one way would be to drop the pan, then apply power and ground to the connection on the case, then listen and feel for the solenoid[s] to activate. that would be my first step. if they both work at the transmission, i would then work backward in the harness to see where the connection breaks. if the solenoid[s] does not work at the transmission case connection, i would then go directly to that solenoid with power and ground. if it then works, the wiring to the case connector needs repaired. if the solenoid doesn't work, it needs replaced. just my way of doing things. your mileage will vary.
|
|
|
Re: 518 OD not engaging
[Re: BDW]
#3091892
11/05/22 08:10 PM
11/05/22 08:10 PM
|
Joined: Dec 2009
Posts: 20,700 in a cattle trailer down by th...
Guitar Jones
Paddle faster! I hear banjo music!
|
Paddle faster! I hear banjo music!
Joined: Dec 2009
Posts: 20,700
in a cattle trailer down by th...
|
What if the solenoid is good, what else could go bad?
What does the OD solenoid activate, is there a clutch pack or something, what changes the ratio? I think the OD circuit was miswired so the OD was hardwired to ground.
Would it be possible to hear the solenoids activate through the pan, before it’s removed?
Appreciate the replies I have never been able to hear them. You can remove the o/d ground, key on o/d switch on check for voltage at the ground wire. There should be voltage there. If not the solenoid or wire is open.
"Follow me the wise man said, but he walked behind"
'92 D250 Club Cab CTD, 47RH conversion, pump tweaks, injectors, rear disc and hydroboost conversion. '74 W200 Crew Cab 360, NV4500, D44, D60 and NP205 divorced transfer case. Rear disc and hydroboost conversion. 2019 1500 Long Horn Crew Cab 4WD, 5.7 Hemi.
|
|
|
Re: 518 OD not engaging
[Re: BDW]
#3091995
11/06/22 01:11 PM
11/06/22 01:11 PM
|
Joined: Jan 2004
Posts: 8,374 fredericksburg,va
cudaman1969
master
|
master
Joined: Jan 2004
Posts: 8,374
fredericksburg,va
|
What if the solenoid is good, what else could go bad?
What does the OD solenoid activate, is there a clutch pack or something, what changes the ratio? I think the OD circuit was miswired so the OD was hardwired to ground.
Would it be possible to hear the solenoids activate through the pan, before it’s removed?
Appreciate the replies The solinoid activates the valve with the big spring and piston in valve body, have to look at a diagram on internet. Once activated the overdrive clutch pac engages. That’s in the tail housing. If that’s gone major linning pieces in the pan
|
|
|
Re: 518 OD not engaging
[Re: cudaman1969]
#3092006
11/06/22 01:52 PM
11/06/22 01:52 PM
|
Joined: May 2005
Posts: 4,762 Florida
BDW
OP
master
|
OP
master
Joined: May 2005
Posts: 4,762
Florida
|
Well, now I'm worried, did the 2 tests mentioned above,
Disconnected all wiring so there is 12V to center pin and the 2 outside wires are not connected to anything.
1) measured resistance between center pin, and it's 36ohms for both LU and OD. 2) feed 12V to center pin, measured LU and OD side to ground, they are both 12V.
So that seems to indicated that both solenoids are ok? Did a google search and it looks like solenoids are basically a coil winding and should be a DC short.
So unless the other side, magnetic plunger in the solenoid is bad, I've got bigger issues.
|
|
|
Re: 518 OD not engaging
[Re: BDW]
#3092009
11/06/22 02:08 PM
11/06/22 02:08 PM
|
Joined: Mar 2011
Posts: 3,113 Michigan
A727Tflite
master
|
master
Joined: Mar 2011
Posts: 3,113
Michigan
|
Well, now I'm worried, did the 2 tests mentioned above,
Disconnected all wiring so there is 12V to center pin and the 2 outside wires are not connected to anything.
1) measured resistance between center pin, and it's 36ohms for both LU and OD. 2) feed 12V to center pin, measured LU and OD side to ground, they are both 12V.
So that seems to indicated that both solenoids are ok? Did a google search and it looks like solenoids are basically a coil winding and should be a DC short.
So unless the other side, magnetic plunger in the solenoid is bad, I've got bigger issues.
Did you try to see if you had OD pressure? Report back your findings. If the solenoid is truly good, first thing to look for is a stuck OD control valve, which lies underneath that solenoid.
|
|
|
Re: 518 OD not engaging
[Re: A727Tflite]
#3092060
11/06/22 05:50 PM
11/06/22 05:50 PM
|
Joined: May 2005
Posts: 4,762 Florida
BDW
OP
master
|
OP
master
Joined: May 2005
Posts: 4,762
Florida
|
Did you try to see if you had OD pressure? Report back your findings.
If the solenoid is truly good, first thing to look for is a stuck OD control valve, which lies underneath that solenoid.
[/quote] I don't have a pressure gauge, but I know it must put out 50lbs around 50mph. My home brew controller has a pressure switch that activates at 50mph, LU still works, the OD just isn't kicking in. I took car for a test run, for another issue I'm chasing, and tested both the LU and OD with the manual switches (only above 50mph) Randomly toggling the OD switch and it did kick in (1 time) and the RPMs dropped as expected and ran fine until I had to stop for light. OD never came back on, but LU always works. So at this point I'm thinking my next step is to just bite the bullet and attempt to change the solenoid. Any other options? Any harm in driving it as is, and just use the LU above 50mph? Thx
Last edited by BDW; 11/06/22 05:50 PM.
|
|
|
Re: 518 OD not engaging
[Re: BDW]
#3092064
11/06/22 06:11 PM
11/06/22 06:11 PM
|
Joined: May 2005
Posts: 4,762 Florida
BDW
OP
master
|
OP
master
Joined: May 2005
Posts: 4,762
Florida
|
Additional bit of info, random or related, no idea? I just swapped in a new motor that took me a year to get finished. It's seems like forever ago, but OD worked before I started the engine swap. But it's hard to remember, and most of my driving probably didn't require OD. This transmission was a JY pull 7 years ago, and was completely rebuilt with Transgo shift kit. It has run flawless for the last 7 years, and only has 15k miles on it since then.
So the transmission has been sitting (in car, in garage) for 1 year, and just randomly craps out when I take car out for first test drive with new engine........................
|
|
|
Re: 518 OD not engaging
[Re: BDW]
#3092153
11/06/22 09:46 PM
11/06/22 09:46 PM
|
Joined: Mar 2011
Posts: 3,113 Michigan
A727Tflite
master
|
master
Joined: Mar 2011
Posts: 3,113
Michigan
|
Did you try to see if you had OD pressure? Report back your findings.
If the solenoid is truly good, first thing to look for is a stuck OD control valve, which lies underneath that solenoid.
I don't have a pressure gauge, but I know it must put out 50lbs around 50mph. My home brew controller has a pressure switch that activates at 50mph, LU still works, the OD just isn't kicking in. I took car for a test run, for another issue I'm chasing, and tested both the LU and OD with the manual switches (only above 50mph) Randomly toggling the OD switch and it did kick in (1 time) and the RPMs dropped as expected and ran fine until I had to stop for light. OD never came back on, but LU always works. So at this point I'm thinking my next step is to just bite the bullet and attempt to change the solenoid. Any other options? Any harm in driving it as is, and just use the LU above 50mph? Thx Driving in third with or w/o lockup will not hurt it a bit. The fact you got o/d makes me think a band solenoid. But could be several things. Setting for a long time shouldn’t have an impact on it. Driver side pressure tap above rear cooler line is O/D pressure tap. The one on the pass. side is governor. You should have no more than 5 psi until O/D is activated. You mention 50 psi. You may be reading the gov psi - that follows road speed. [/quote]
|
|
|
Re: 518 OD not engaging
[Re: BDW]
#3092420
11/07/22 09:35 PM
11/07/22 09:35 PM
|
Joined: Mar 2011
Posts: 3,113 Michigan
A727Tflite
master
|
master
Joined: Mar 2011
Posts: 3,113
Michigan
|
Looks like only 2 manufacturers for the solenoid. Any thoughts on which might be better, seems like a simple part, curious why ATP is 2x the cost
ATP for $60 Sonnax/Rostra for $30 Have you checked what the dealer has for OE Mopar solenoids?
|
|
|
Re: 518 OD not engaging
[Re: A727Tflite]
#3092426
11/07/22 10:02 PM
11/07/22 10:02 PM
|
Joined: Jan 2004
Posts: 8,374 fredericksburg,va
cudaman1969
master
|
master
Joined: Jan 2004
Posts: 8,374
fredericksburg,va
|
Looks like only 2 manufacturers for the solenoid. Any thoughts on which might be better, seems like a simple part, curious why ATP is 2x the cost
ATP for $60 Sonnax/Rostra for $30 Have you checked what the dealer has for OE Mopar solenoids? What I would do too, there’s a reason for low price
|
|
|
|
|