Previous Thread
Next Thread
Print Thread
Page 3 of 3 1 2 3
Re: 64 Dodge went to the track last night [Re: B1Fish540] #422618
07/31/09 09:47 PM
07/31/09 09:47 PM
Joined: Dec 2003
Posts: 1,401
Wi.
old_racer Offline
pro stock
old_racer  Offline
pro stock

Joined: Dec 2003
Posts: 1,401
Wi.
Hi
do you plan on bringing it to the nats? , stop by us in the pits and we'll help you tune or what ever you need.
Russ

Re: 64 Dodge went to the track last night [Re: old_racer] #422619
07/31/09 10:40 PM
07/31/09 10:40 PM
Joined: Jan 2008
Posts: 449
Wisconsin
sjs64polara Offline OP
mopar
sjs64polara  Offline OP
mopar

Joined: Jan 2008
Posts: 449
Wisconsin
Quote:

Hi
do you plan on bringing it to the nats? , stop by us in the pits and we'll help you tune or what ever you need.
Russ




Yes we are going.....
I appreciate the gesture, I may take you up on that.
I have a lot of learning to do

5389618-Polara13.jpg (70 downloads)
Re: 64 Dodge went to the track last night [Re: B1Fish540] #422620
07/31/09 10:51 PM
07/31/09 10:51 PM
Joined: Jan 2008
Posts: 449
Wisconsin
sjs64polara Offline OP
mopar
sjs64polara  Offline OP
mopar

Joined: Jan 2008
Posts: 449
Wisconsin
Quote:

Quote:

Standard port, 906 heads with Rick Allison intake




Do you know how the heads flowed? I know its hard to get them much over 250-265 CFM with out making them crack. My point is, you may not be making as much HP as you think simply because the heads wont support it. Your cam should work good with those heads, but being only in the .540 lift area would also limit HP. But that said, I too think you should run mid 11s easy...like was mentioned with all that TQ you may need a tighter convertor.




No I dont know how the heads flowed but I do have a lot of dyno data.

Dynamic just told me how to check the flash so I'll check that out over the next few days. A&A had them set for 3400 so I'll see how close it is

Ya think my burn out is a little much for Hoosier DOT drag radials I kinda thought I was John Force for a few seconds

Re: 64 Dodge went to the track last night [Re: sjs64polara] #422621
08/02/09 11:10 AM
08/02/09 11:10 AM
Joined: Jan 2008
Posts: 449
Wisconsin
sjs64polara Offline OP
mopar
sjs64polara  Offline OP
mopar

Joined: Jan 2008
Posts: 449
Wisconsin
Dynamic just told me how to check the flash so I'll check that out over the next few days. A&A had them set for 3400 so I'll see how close it is


Just checked the flash on my 9 1/2 " Dynamic..... I put it in 3rd, rolled about 5 mph and gunned it. The tach went to 3000rpm. I did it a few times, the rpms dropped a little every time Then rechecked it by puttingg it in 3rd, stopped the car, held the brake then quick punched it, about 3000 again.

So with that said, what should I leave the line at? When I try and leave at 2200-2300 RPM, the tires spin before the light even goes green and then I look like a DA

5392271-takeoff.jpg (70 downloads)
Re: 64 Dodge went to the track last night #422622
08/02/09 11:42 AM
08/02/09 11:42 AM
Joined: Sep 2008
Posts: 2,840
Flint, Michigan
B1Fish540 Offline
master
B1Fish540  Offline
master

Joined: Sep 2008
Posts: 2,840
Flint, Michigan
Quote:

Quote:

Dyno'd with manifolds and switched to 2" TTI's becasue of heat issues.

I agree, I need seat time, practice with burn outs and launches




if you switched to TTI's after the dyno session, i would definitely shift the car around 5800-6000 and i bet you see a slight pickup of about 5 hundredths.to probably a .1
i did with almost the same combo.
also change out that converter to at least a 4000-4500 stall.




I mis read your cam lift..i see its over .560 so maybe you dont have enough stall..i would say 4000 or 4500 would be closer like SS says. Not being able to hold the car sounds familiar, my challenger did the same thing until I went to a Coan. You might consider trying a different convertor, I had a 3000 stall J.W. that felt just like stock. Went to the 3500 Coan and could hold the car at 3000 rpm with my stock drum brakes.

Page 3 of 3 1 2 3






Powered by UBB.threads™ PHP Forum Software 7.7.1