Originally Posted by Dave_J
When I bought my 78 LRT in 1994 it was going cheap. I was the 5th person to look and test drive it. It ran like crap.
I paid the $1200 cash and drove it the 12 miles home and it was way down on power. Doing 45 MPH, I lost speed climbing a long hill going home. I parked it for a week. This is when I found out the engine was a 1978 Warranty replacement E58.

I pulled a compression test and all were at about 145 PSI but #3 was way down, like 80 PSI WET.
Took the valve cover off and found the #3 intake rocker's push rod cup was broken out, windowed but still attached. Push rod was OK but the lifter was almost popped out of its bore. Using my 2.2 coil spring compressor I could push the valve down with no binding. Took a spare rocker and put it back together. Ran excellent. Never another issue in the 200,000 miles I drove it


Had exact same issue with a 75 dart 4door 318 . . ran like crap . . .pulled left hand valve cover - yup, one rocker arm had pushrod through it . . . took old rocker from another head, pushrod was still ok, buttoned up and ran like champ !! Gotta love those cheap fixes ! Think I paid $350 for the car, and put another $350 into it (tires, brakes) and drove it for a few years, and sold for $1k ! . .