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Re: Fuel flow thru reg? [Re: emarine01] #1453797
06/18/13 09:40 PM
06/18/13 09:40 PM
Joined: May 2011
Posts: 4,489
northern,Ohio,USA
C
Clanton Offline
master
Clanton  Offline
master
C

Joined: May 2011
Posts: 4,489
northern,Ohio,USA
LOL go have some fun now!


GOTBOOST!New improved with Victor heads.
http://www.enginelabs.com/mopar-big-bloc...t-of-necessity/
Re: Fuel flow thru reg? [Re: emarine01] #1453798
06/19/13 01:56 AM
06/19/13 01:56 AM
Joined: Jul 2004
Posts: 19,317
State of confusion
T
Thumperdart Offline
I Live Here
Thumperdart  Offline
I Live Here
T

Joined: Jul 2004
Posts: 19,317
State of confusion
Quote:

2 6an lines one off each reg port to each bowl seems to have solved the problem, But she source of the problem was a kinked line @ the 90* bend to the front bowl that was hidden by the SS cover on the fuel line, When I did the flow testing I dropped that line and straightened out the 90 to go in the bucket thus fixing the kink, I found the kink from cutting the line to shorten it This was nothing but a frustrating fire drill where the testing made no sense, Thankx to all for the help.


Been there............can drive you nutser for sure but hey you found it.

Last edited by Thumperdart; 06/19/13 01:57 AM.

72 Dart 470 n/a BB stroker street car `THUMPER`...Check me out on FB Dominic Thumper for videos and lots of carb pics......760-900-3895.....
Re: Fuel flow thru reg? [Re: Thumperdart] #1453799
06/19/13 11:31 AM
06/19/13 11:31 AM
Joined: Nov 2004
Posts: 7,274
s.w.fl
B
bonefish Offline
master
bonefish  Offline
master
B

Joined: Nov 2004
Posts: 7,274
s.w.fl
thats the kinda stuff that happens to me.just went thru the same thing with a coil wire.worked great when i grounded it out but put it back no spark.changed coils ,dist,finally figered it out.

Re: Fuel flow thru reg? [Re: emarine01] #1453800
06/19/13 02:35 PM
06/19/13 02:35 PM
Joined: Aug 2003
Posts: 43,173
Bend,OR USA
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Cab_Burge Offline
I Win
Cab_Burge  Offline
I Win
C

Joined: Aug 2003
Posts: 43,173
Bend,OR USA
Quote:

2 6an lines one off each reg port to each bowl seems to have solved the problem, But she source of the problem was a kinked line @ the 90* bend to the front bowl that was hidden by the SS cover on the fuel line, When I did the flow testing I dropped that line and straightened out the 90 to go in the bucket thus fixing the kink, I found the kink from cutting the line to shorten it This was nothing but a frustrating fire drill where the testing made no sense, Thankx to all for the help.


Lots of gremlins out there, the simple stuff will kill you trying to find it


Mr.Cab Racing and winning with Mopars since 1964. (Old F--t, Huh)
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