Re: Leak Down Test Problem on #2 Cylinder
[Re: n20mstr]
#2970977
10/05/21 02:57 PM
10/05/21 02:57 PM
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Joined: Dec 2013
Posts: 4,672 Wichita
GY3
master
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master
Joined: Dec 2013
Posts: 4,672
Wichita
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Yikes! And here I figured the cast crank would be the first to go!
How much boost were you throwing at it?
'63 Dodge 330 11.19 @ 121 mph Pump gas, n/a, through the mufflers on street tires with 3.54's. 3,600 lbs. 10.01 @ 133mph with a 250 shot of nitrous an a splash of race gas. 1.36 60 ft. 3,700 lbs.
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Re: Leak Down Test Problem on #2 Cylinder
[Re: n20mstr]
#2970986
10/05/21 03:11 PM
10/05/21 03:11 PM
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Joined: Jan 2003
Posts: 13,360 Marion, South Carolina [><]
an8sec70cuda
I Live Here
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I Live Here
Joined: Jan 2003
Posts: 13,360
Marion, South Carolina [><]
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Ring Gap looks to be a little too big. Thats why your leakdown was excessive Only to be made worse by the too large gas porting.
CHIP '70 hemicuda, 575" Hemi, 727, Dana 60 '69 road runner, 440-6, 18 spline 4 speed, Dana 60 '71 Demon, 340, low gear 904, 8.75 '73 Chrysler New Yorker, 440, 727, 8.75 '90 Chevy 454SS Silverado, 476" BBC, TH400, 14 bolt '06 GMC 2500HD LBZ Duramax
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Re: Leak Down Test Problem on #2 Cylinder
[Re: Cab_Burge]
#2971080
10/05/21 06:17 PM
10/05/21 06:17 PM
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Joined: Mar 2011
Posts: 3,074 Michigan
A727Tflite
master
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master
Joined: Mar 2011
Posts: 3,074
Michigan
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Not sure where that piston came from originally, doesn’t look at all like this Chinese piston.
😂. Ah So.
Last edited by Transman; 10/06/21 10:26 AM.
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Re: Leak Down Test Problem on #2 Cylinder
[Re: Blusmbl]
#2971129
10/05/21 08:50 PM
10/05/21 08:50 PM
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Joined: Feb 2005
Posts: 20,172 PA.
pittsburghracer
"Little"John
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"Little"John
Joined: Feb 2005
Posts: 20,172
PA.
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Wholly meltdown Batman!! Sorry to see that.
1970 Duster Edelbrock headed 408 5.984@112.52 422 Indy headed small block 5.982@112.56 mph 9.42@138.27
Livin and lovin life one day at a time
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Re: Leak Down Test Problem on #2 Cylinder
[Re: dvw]
#2971250
10/06/21 09:01 AM
10/06/21 09:01 AM
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Joined: Jan 2005
Posts: 3,635 Oakland, MI
dizuster
OP
master
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OP
master
Joined: Jan 2005
Posts: 3,635
Oakland, MI
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It actually shocks me how little it was smoking for how big that hole was!!!!
What you're looking at is a custom made Diamond Piston specific for my turbo application. 2818 material, Thick crown, ring is down a bunch, etc... Certainly no fault of the piston.
It had hurt the converter at Monster Mopar earlier this year, and wouldn't 60ft at all. So I was leaning on the tune pretty hard to get it to run 10.0 for the shootout (about 20-21psi of boost). Went 9.98@139.7mph on the last pass.
It's a little bit strange because the A/F wasn't excessively lean on the data logger, nor do any of the other cylinders look like they had anything wrong with them. #1 and #2 cylinders always run the hottest on this car, so as I was adding boost/timing, I was watching #1 carefully. Whoops... should have been watching #2 apparently!
We will see if the block is going to clean up. Hopefully I can just slap another set of pistons in it and go... but we'll see.
It is absolutely amazing to me that the piston can take that kind of abuse, and the stock block/cast crank still survives!!!!
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Re: Leak Down Test Problem on #2 Cylinder
[Re: GomangoCuda]
#2971386
10/06/21 03:39 PM
10/06/21 03:39 PM
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Joined: Jan 2005
Posts: 3,635 Oakland, MI
dizuster
OP
master
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OP
master
Joined: Jan 2005
Posts: 3,635
Oakland, MI
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Sharp edge on the valve notch likely caused that. I 100% agree. No doubt the radial edge of the valve pocket makes this the thinnest area. I hand "massaged" these the best I could to minimize any sharp edge, but at the end of the day every part has a weak point somewhere. Running standard off the shelf Cometics.
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