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Leak Down Test Problem on #2 Cylinder #2970959
10/05/21 02:29 PM
10/05/21 02:29 PM
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Oakland, MI
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dizuster Offline OP
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Anybody got some JB weld or a caulk gun I can borrow? Seems like I need to make a minor repair to #2 piston.

Melted PIston.jpgMelted Piston Bore.png
Re: Leak Down Test Problem on #2 Cylinder [Re: dizuster] #2970976
10/05/21 02:56 PM
10/05/21 02:56 PM
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On the parachute mount
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n20mstr Offline
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On the parachute mount
Ring Gap looks to be a little too big. Thats why your leakdown was excessive


....BAD A$$ STREET CAR.....
Re: Leak Down Test Problem on #2 Cylinder [Re: n20mstr] #2970977
10/05/21 02:57 PM
10/05/21 02:57 PM
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Wichita
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GY3 Offline
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Yikes! And here I figured the cast crank would be the first to go!

How much boost were you throwing at it?


'63 Dodge 330
11.19 @ 121 mph
Pump gas, n/a, through the mufflers on street tires with 3.54's. 3,600 lbs.
10.01 @ 133mph with a 250 shot of nitrous an a splash of race gas. 1.36 60 ft. 3,700 lbs.

Re: Leak Down Test Problem on #2 Cylinder [Re: n20mstr] #2970986
10/05/21 03:11 PM
10/05/21 03:11 PM
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Marion, South Carolina [><]
an8sec70cuda Offline
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Originally Posted by n20mstr
Ring Gap looks to be a little too big. Thats why your leakdown was excessive

iagree Only to be made worse by the too large gas porting.


CHIP
'70 hemicuda, 575" Hemi, 727, Dana 60
'69 road runner, 440-6, 18 spline 4 speed, Dana 60
'71 Demon, 340, low gear 904, 8.75
'73 Chrysler New Yorker, 440, 727, 8.75
'90 Chevy 454SS Silverado, 476" BBC, TH400, 14 bolt
'06 GMC 2500HD LBZ Duramax
Re: Leak Down Test Problem on #2 Cylinder [Re: dizuster] #2971008
10/05/21 03:51 PM
10/05/21 03:51 PM
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Bend,OR USA
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Cab_Burge Offline
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Originally Posted by dizuster
Anybody got some JB weld or a caulk gun I can borrow? Seems like I need to make a minor repair to #2 piston.


Welcome to the I broke parts racing club whistling
Time to get to work to make it stronger so it will take more abuse and make more power wrench devil up
Sorry for your loss twocents


Mr.Cab Racing and winning with Mopars since 1964. (Old F--t, Huh)
Re: Leak Down Test Problem on #2 Cylinder [Re: Cab_Burge] #2971080
10/05/21 06:17 PM
10/05/21 06:17 PM
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Michigan
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A727Tflite Online content
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Michigan
Not sure where that piston came from originally, doesn’t look at all like this Chinese piston.

😂. Ah So.

C8C0E43A-036C-4D42-AAC5-4D207CEBBF59.jpeg
Last edited by Transman; 10/06/21 10:26 AM.
Re: Leak Down Test Problem on #2 Cylinder [Re: A727Tflite] #2971088
10/05/21 06:55 PM
10/05/21 06:55 PM
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Posts: 8,164
Plymouth, MI
Blusmbl Offline
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There are better ways to reduce the compression ratio! shock


'18 Ford Raptor, random motorcycles, 1968 Plymouth Fury III - 11.37 @ 118
Re: Leak Down Test Problem on #2 Cylinder [Re: Blusmbl] #2971129
10/05/21 08:50 PM
10/05/21 08:50 PM
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PA.
pittsburghracer Offline
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PA.


Wholly meltdown Batman!! Sorry to see that.


1970 Duster
Edelbrock headed 408
5.984@112.52
422 Indy headed small block
5.982@112.56 mph
9.42@138.27

Livin and lovin life one day at a time




Re: Leak Down Test Problem on #2 Cylinder [Re: dizuster] #2971137
10/05/21 09:03 PM
10/05/21 09:03 PM
Joined: Jan 2003
Posts: 1,020
Andrews,In. U.S.of A.
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67_Satellite Offline
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Andrews,In. U.S.of A.
I have nightmares that end looking like that.

Re: Leak Down Test Problem on #2 Cylinder [Re: 67_Satellite] #2971158
10/05/21 09:45 PM
10/05/21 09:45 PM
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Michigan
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Did it launch a breather off the valve cover when this happened ?

Re: Leak Down Test Problem on #2 Cylinder [Re: A727Tflite] #2971194
10/05/21 11:11 PM
10/05/21 11:11 PM
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West Plains, MO
DrCharles Offline
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Originally Posted by Transman
Not sure where that piston came from originally, doesn’t look at all like this Chinese piston.


That one looks more like the head came off a Chinese valve and beat the crap out of the piston and cylinder head? scope

Re: Leak Down Test Problem on #2 Cylinder [Re: DrCharles] #2971204
10/06/21 12:15 AM
10/06/21 12:15 AM
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Bend,OR USA
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Cab_Burge Offline
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Broken valves don't normally melt aluminum, especially like this one did twocentswork


Mr.Cab Racing and winning with Mopars since 1964. (Old F--t, Huh)
Re: Leak Down Test Problem on #2 Cylinder [Re: Cab_Burge] #2971211
10/06/21 01:11 AM
10/06/21 01:11 AM
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Northern Bavaria / Germany
MichaelF Offline
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Northern Bavaria / Germany
ouch....lean condition under boost?

Re: Leak Down Test Problem on #2 Cylinder [Re: A727Tflite] #2971212
10/06/21 01:24 AM
10/06/21 01:24 AM
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Indiana
Gabby63 Offline
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Indiana
That piston has Holloween all over it , lol Gary

Re: Leak Down Test Problem on #2 Cylinder [Re: Gabby63] #2971231
10/06/21 07:50 AM
10/06/21 07:50 AM
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MI, usa
dvw Offline
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Funny thing was it was barely smoking out the exhaust after a 139.7 mph pass. No oil out of the breather.
Doug

Re: Leak Down Test Problem on #2 Cylinder [Re: dvw] #2971250
10/06/21 09:01 AM
10/06/21 09:01 AM
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Oakland, MI
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dizuster Offline OP
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It actually shocks me how little it was smoking for how big that hole was!!!!

What you're looking at is a custom made Diamond Piston specific for my turbo application. 2818 material, Thick crown, ring is down a bunch, etc... Certainly no fault of the piston.

It had hurt the converter at Monster Mopar earlier this year, and wouldn't 60ft at all. So I was leaning on the tune pretty hard to get it to run 10.0 for the shootout (about 20-21psi of boost). Went 9.98@139.7mph on the last pass.

It's a little bit strange because the A/F wasn't excessively lean on the data logger, nor do any of the other cylinders look like they had anything wrong with them. #1 and #2 cylinders always run the hottest on this car, so as I was adding boost/timing, I was watching #1 carefully. Whoops... should have been watching #2 apparently!

We will see if the block is going to clean up. Hopefully I can just slap another set of pistons in it and go... but we'll see.


It is absolutely amazing to me that the piston can take that kind of abuse, and the stock block/cast crank still survives!!!!


Re: Leak Down Test Problem on #2 Cylinder [Re: dizuster] #2971260
10/06/21 09:47 AM
10/06/21 09:47 AM
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Moved to N.E. Tennessee
GomangoCuda Offline
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Sharp edge on the valve notch likely caused that.


In theory, there is no difference between theory and practice. In practice, there is.
Re: Leak Down Test Problem on #2 Cylinder [Re: GomangoCuda] #2971294
10/06/21 11:46 AM
10/06/21 11:46 AM
Joined: Dec 2018
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Northern Bavaria / Germany
MichaelF Offline
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What Kind of head gasket do you run with this Engine?

Re: Leak Down Test Problem on #2 Cylinder [Re: Cab_Burge] #2971385
10/06/21 03:38 PM
10/06/21 03:38 PM
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Posts: 4,220
West Plains, MO
DrCharles Offline
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West Plains, MO
Originally Posted by Cab_Burge
Broken valves don't normally melt aluminum, especially like this one did twocentswork

I thought it was pretty obvious I was referring to Transman's piston pic, not the OP's melted one... shruggy
This one:
[Linked Image]

Re: Leak Down Test Problem on #2 Cylinder [Re: GomangoCuda] #2971386
10/06/21 03:39 PM
10/06/21 03:39 PM
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Oakland, MI
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dizuster Offline OP
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Originally Posted by GomangoCuda
Sharp edge on the valve notch likely caused that.


I 100% agree. No doubt the radial edge of the valve pocket makes this the thinnest area. I hand "massaged" these the best I could to minimize any sharp edge, but at the end of the day every part has a weak point somewhere.


Running standard off the shelf Cometics.

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