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Re: trouble shooting stock 383 issue
[Re: GOLDMYN]
#2184541
10/28/16 02:40 PM
10/28/16 02:40 PM
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Joined: Aug 2004
Posts: 1,960 Kenosha, Wi
GOLDMYN
OP
top fuel
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OP
top fuel
Joined: Aug 2004
Posts: 1,960
Kenosha, Wi
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Tank was in serviceable condition, but since I had it out I believe in prevention rather than trouble years from now when it'll be impossible to find someone who seals tanks, The way it was, there was no one in the town I live in, people look at you like your from Mars.
Semper Fi
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Re: trouble shooting stock 383 issue
[Re: GOLDMYN]
#2184618
10/28/16 03:46 PM
10/28/16 03:46 PM
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Joined: Jan 2004
Posts: 9,066 Eugene, Oregon
minivan
master
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master
Joined: Jan 2004
Posts: 9,066
Eugene, Oregon
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UPDATE. Changed the points/condenser and problem solved. I knew a good mechanic in 71 who could not get a car to run right no matter what he did... Common thing back then was to change the points but leave the condenser... After trying everything he knew in installed a new condenser, problem solved.. Your post ending made me think of this.....
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Re: trouble shooting stock 383 issue
[Re: GOLDMYN]
#2184951
10/28/16 10:58 PM
10/28/16 10:58 PM
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Joined: Jan 2003
Posts: 5,467 So Cal
Sinitro
master
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master
Joined: Jan 2003
Posts: 5,467
So Cal
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Check the bulkhead wiring connectors (3)... After 50 years they get corroded and oxidized.. Pop them apart, burnish the contacts, recrimp the female tab conectors on the firewall side, coat with dia-electric grease and reinstall... Just my $0.02...
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Re: trouble shooting stock 383 issue
[Re: Sinitro]
#2185148
10/29/16 09:07 AM
10/29/16 09:07 AM
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Joined: Aug 2004
Posts: 1,960 Kenosha, Wi
GOLDMYN
OP
top fuel
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OP
top fuel
Joined: Aug 2004
Posts: 1,960
Kenosha, Wi
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Check the bulkhead wiring connectors (3)... After 50 years they get corroded and oxidized.. Pop them apart, burnish the contacts, recrimp the female tab conectors on the firewall side, coat with dia-electric grease and reinstall... Just my $0.02... ? problem solved
Semper Fi
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