BB 727 woes
#1953791
11/18/15 05:45 PM
11/18/15 05:45 PM
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Joined: Mar 2005
Posts: 119 Jacksonville , Fl
Volare4life
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So I finally got the 400BB in the volare running like a beast, but now I am having issues with the trans, reverse is really sluggish to the point of high rpms to move, and 3rd gear sounds like its free revving. I modified the valve body per the transgo TF-2 instructions for the street strip with shift command, I know that the valve body is good to go, since its the same one i had in my boosted slant and that thing was a beast, and shifted gears just fine, I am thinking that maybe the front band might need tightening up, since the transgo instructions say tighten till snug then back off 2 turns.....whats snug ? lol any advice or help is greatly appreciated, first and second shift no issues in auto and manual mode ( courtesy of my hurst V-matic 2) but no thrid just a high whine and like i already said reverse works but high rpms to make her move. also installed my own cable kickdown, used the buchillon for inspiration, and adjusted per there instructions,
Thanks, -Mike
The answers are out there you just got to look hard enough
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Re: BB 727 woes
[Re: Volare4life]
#1953820
11/18/15 06:49 PM
11/18/15 06:49 PM
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Joined: May 2003
Posts: 1,751 Graham, WA
Polarapete
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top fuel
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In my world "snug" is more than "Finger tight" and less than "Tight". Now I don't mean to be a smart ass, it is just a matter of feel.
If you had the trans out of the car you probably would roll over the front drum and tighten the band until it dragged or even would not roll anymore, then back off the 2 or 3 turns on the adjusting screw and tighten the locknut. And do the same on the rear band. Make sure the filter screen is clean and that the fluid is up to proper level cause you may just be lacking fluid.
1986 Dodge Ramcharger 440 2wd, Bracket Racer Under Construction 1998 Ram 2500 QuadCab, new daily driver. 2008 Honda Element 2014 Carry-On 7x14 Cargo Trailer
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Re: BB 727 woes
[Re: Volare4life]
#1953956
11/18/15 10:20 PM
11/18/15 10:20 PM
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Joined: Mar 2005
Posts: 119 Jacksonville , Fl
Volare4life
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dvw- Yes i did install the cupped orifice plug in the trans, I was told the trans functioned right up to being pulled and stored, I never ran it with the stock valve body, just my modified one. Not rebuilt to my knowledge
Polarapete- that's exactly how I did it with the trans out and doing the transgo mods, also had my handy "torqueflite A-727" by Carl H. Munroe at my side since he does the exact mods in the transgo kit in the book, I triple checked the fluid and the levels looked good, maybe a bit above the dipstick full reading, I don't think a bit over the line could cause these issues, and from what ya'll have said and a bit more research its really looking like front clutch issues, gonna readjust the front band and see if it helps at all, I am hoping i might have been on the loose side of snug,
-Mike
The answers are out there you just got to look hard enough
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Re: BB 727 woes
[Re: Volare4life]
#1954058
11/19/15 12:39 AM
11/19/15 12:39 AM
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Joined: Mar 2005
Posts: 119 Jacksonville , Fl
Volare4life
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Should I remove that orifice plug when i drop the valve body ? I am pretty sure I didn't have it in my 904/ turbo 225 setup, yea just read in the instructions, ONLY for 727's, so is it really a necessary item to install ? book says only about 25-30 psi, will that be enough psi to test ?
-Mike
The answers are out there you just got to look hard enough
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Re: BB 727 woes
[Re: Volare4life]
#1954363
11/19/15 04:47 PM
11/19/15 04:47 PM
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Joined: Jan 2003
Posts: 74,974 U.S.S.A.
JohnRR
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I was told the trans functioned right up to being pulled and stored, I never ran it with the stock valve body, just my modified one. Not rebuilt to my knowledge -Mike So you know basically NOTHING about this trans . The symptoms point to a problem with the front clutch pack, taking the plug out is not going to fix it. I see a crash course in rebuilding a 727 in your future.
running up my post count some more .
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Re: BB 727 woes
[Re: Volare4life]
#1955447
11/21/15 05:46 PM
11/21/15 05:46 PM
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Joined: Mar 2005
Posts: 119 Jacksonville , Fl
Volare4life
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well I adjusted the kickdown band took it out, had reverse, but no third at all, then once it got warm ( driving around the neighborhood) still no third and reverse started slipped and shuddering, so it looks like shes gonna be coming out.............not fun in a cramped Volare, torn down and rebuilt.... but first to test the front clutch pressure feed hole just to eliminate that, any recommendations for who to go through for parts to rebuild the trans ? I really wasn't looking to sink a ton into it, I have been planning to swap a T-56 in come tax return in January/February time frame, other wise its gonna be an automatic for a bit longer,
-Mike
The answers are out there you just got to look hard enough
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Re: BB 727 woes
[Re: Volare4life]
#1956285
11/23/15 02:33 AM
11/23/15 02:33 AM
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Joined: Mar 2005
Posts: 119 Jacksonville , Fl
Volare4life
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any benefit if I go with 5 thin red vs 4 normal thickness clutches ?Ho w do you know if you have a high gear drum ? Also I am leaning more towards A&A for the parts, but also hear a lot of great things about CRT, but then again turbo action is local to me, anyone have experience with the turbo action tranz box rebuild kit ? Also the A&A kit is only $150 vs the TA tranz box at $314 (on jegs), judging by the description they include the same parts,
-Mike
The answers are out there you just got to look hard enough
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Re: BB 727 woes
[Re: Volare4life]
#1958987
11/27/15 10:32 PM
11/27/15 10:32 PM
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Joined: Nov 2003
Posts: 36,040 Lincoln Nebraska
RapidRobert
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this might not even apply to the prob at hand but a FYI I could not get my bands to torque to 72 INCH lbs (then back off several turns of course). I kept going tighter and tighter to where I knew I had to stop & regroup before I broke something. Kunkel had me set the gap(s) to 1/4 and 5/16 (I forget which was the front and rear) as that is the bottom line just like valve lash. (904) Holler how things turn out.
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Re: BB 727 woes
[Re: Volare4life]
#1959030
11/27/15 11:52 PM
11/27/15 11:52 PM
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Joined: Mar 2005
Posts: 119 Jacksonville , Fl
Volare4life
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I'll post a pic of the band, but there is no deformation or cracks, the band material still looks good, slight discoloration on the steel band itself, but i think that is from sitting the "god knows how long it had been, owner swapped it for an 833 xx years ago....
Last edited by Volare4life; 11/27/15 11:53 PM.
The answers are out there you just got to look hard enough
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